TraceAxis ConsoleIncident Ops
Current Workspace

Localization drift before aisle merge

Pose confidence degraded during a congested merge. Planner entered recovery, then mission aborted.

Robot
AX-17
Site
Phoenix DC
Version
v0.9.14
Active frame
06:37
Primary Replay

Interactive incident stage

T + 06:37
Forward cameraWaypoint M-14
Planner recovery loop engages

The robot enters recovery mode, holds forward motion, and begins re-localization attempts.

Planner mode recovery
Event: Operator bookmark
Trace: mission_state
Control Trace

Commands and transitions

Replay Timeline

Scrub incident progression

Selected event 07:11
Signals

Telemetry synchronized to cursor

Cursor 06:37
Localization Confidence82
Sample aligned to selected frame
Battery Voltage51
Sample aligned to selected frame
Velocity Command0.8
Sample aligned to selected frame
Event Stream

Anomalies and transitions

Run Metadata
RobotAX-17
SitePhoenix DC
Versionv0.9.14
Selected frame06:37
Cause: Localization Loss
Status: investigating
Inspector

Pinned topics

Preview
{ pose_confidence: 0.51, covariance: 0.18 }
Summary

Root-cause hypothesis

Localization degraded after a moving forklift blocked landmark visibility near waypoint M-14. Planner fallback entered recovery, but pose confidence never recovered before the mission abort threshold.

Primary cause: landmark occlusion
Secondary risk: map shift near M-14
Autonomy Lead2026-04-22 19:58

Planner fallback triggered correctly, but localization confidence never recovered after forklift occlusion.

Perception Engineer2026-04-22 20:11

Need to check whether April map refresh shifted the aisle landmark geometry near waypoint M-14.